Well done on your progress and I could 't make any noises out in your video which worried me.
Why didn't you remove the two PCV bolts which are damaged when you had it stripped down or are you saying your only using two of the four bolts and these damaged bolts aren't in the head?
Thanks, the noise is only really audible from 15 seconds onwards, but it may just be in my head
Out of the four pcv bolts, there are only two holding it on. The other two have had the heads sheer off, with the shafts still remaining in the cam cover. I did look at removing them, but the shaft diameter is so small im not sure an easy out (cente punch and lhs thread bit) would work. Rich suggested using a dremel with a small cutting disk which would slightlt cut the plastic of the valve cover but not too badly and then use a flathead to remove them, but I dont have a cutting disc attachment. Ive left it for now, because it seems to have a good seal even with only two bolts. I did a pcv test with the dipstick and it passed so ive assumed its still functional.
I think now ive done everything I can in a mechanical sense to ensure the engine is working correctly, im going to do some logs to check performance.
I think ill use advanced measuring blocks to measure actual and requested boost, and fuel rail pressure, as well as mass air flow rate and rpm. Any others to measure to help confirm the performance? It is rtech stage one if that bares any relevance.
@dazza you're clued up on this arent you?
Thanks guys