@Pudding thank you very much for such a full detailed process.. exactly what i was hoping for :-) I only see this post today! at which point.. over the weekend, i replaced the cam chain cover gasket (as you know, I done the job twice) and found out afterwards I couldn't use the same gasket.. i think its a 1 trip pony... sooo small oil leak!
possibly related.. and I have to put my hands up here.. but when replacing the gasket, i only went and found that the bottom center bolt of the cam chain cover was loose! last time i must of twizzled it in with the skinny T30 extension by fingers and when torqueing up the 7 bolts.. i must of torqued the T30 right next to it! felt like an absolute plumb mate!!
Anyway, while doing this, cleaning everything up.. I replaced the VVT cam adjuster solenoid. (the sensor going into the cam chain cover) as someone had broken the electrical plug on it previously. I had temporarily repaired it months ago and the car run great! but with the heat, it was brittle and snapped again. so put a new one in and jobs a gooden.
so with all that said.. this weekend I achieved and replaced:
a new VVT cam adjuster solenoid fitted
an oil leak free cam chain cover
an ECU reset as the battery was disconnected for a few hours
a tiny tiny tiny air leak in the bung on the inlet manifold (part of the Forge PCV delete)
took the car for a drive afterwards, once it had warmed up and cam chain had some oil squirted all over and i gotta say.. it drove perfect! more low down grunt.. power just hits and goes.. traction light was wanting to slap me up side the head, and it pulled smoothly all the way through from 2k - 6k! in 2nd and 3rd gear! It bypassed 4k cut off i was getting like it wasn't even a thing!!!
so I'm pleased to say with a mixture of all those, its fixed. whether it was down to a small boost leak, small oil leak loosing crank pressure, dodgy VVT cam adjuster solenoid or what I personally think most of all... is a good ECU reset! whichever the cause, if not a bit of all.. its done and I'm very happy.
my only concern or doubt with the fix.. is my cars been acting very weird in the colder temperatures and the power at 4k could sometimes be intermittent depending on warm or colder conditions. This weekend after the fix, when i drove it was 12 degrees Celsius. so come the colder whether in the next week or 2 i will tell better. no doubt ill be back for more help otherwise haha. (although the way it was behaving.. its fixed
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@bobby_fodge thanks for the suggestion.. as always I'm more than happy for anyone to throw ANY clue or ideas around as it all helps with diagnosis. but the clutch is feeling solid (for now
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thanks again for the input..
@Pudding I am still going to do these logs once i get the chance! just to see if everything is behaving anyway.