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Author Topic: Testing the N80 I just removed...  (Read 893 times)

Offline ROH ECHT

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Testing the N80 I just removed...
« on: June 03, 2020, 05:31:36 pm »
This is just a "show what I found", so here's the N80 I replaced this morning. I tested the new N80 before installing it and the new N80 held vacuum 100%.

There were no fault codes but it has 154k miles on it and has a small fuel additive showing in the fuel trims;

https://www.youtube.com/watch?v=wZ9S...ature=emb_logo

Anyhow, the resistance was just 17.8 ohm on this N80 I removed. The resistance spec is 22 to 30 ohm. So, even though it leaked a bit...it also was likely opening less and causing it to run a bit lean and why my LTFT (partial/multiplicative/off idle) was 7 to 8%. A bit of time and then a data log may show this to be true. I will post more  on the fuel trims after I log it.
« Last Edit: June 03, 2020, 05:34:07 pm by ROH ECHT »
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