Load is fine, n75 values are fine but if you look at the afm values they match the boost actual values.
Something is causing the overboost and its not the ECU requesting it. Actual boost is contolled by the wastegate which is known good as its new. The wastegate is controlled by the N75 valve which is seeing realistic actual values, but that doesnt mean that the n75 is doing as its asked.
I would swap the n75.
P.s thanks for that log of our stg2, other than the issue we are discussing it looks very nice.