Good news is that doms car is now back in 1 piece, test drive / compression test and datalogging tomorrow. List of faults/mistakes found so far:
1 inlet cam out by 30 degrees
2 oil leaking from cam chain casing - no sealent applied to mating faces
3 cambelt cover bolts rounded off
4 exhaust cam end bolt overtightened (should be 25nm + 70 degrees)
5 crankshaft bolt NOT replaced during build
6 over application of sealent to camshaft housing causing loose silicon to drop into cylinderhead
7 excess silicone sealent blocking oil passages in camshaft bearing assembly
8 excess silicon sealent compressed into spark plug apetures in cylinder head
Rounded bolts and all other faults now rectified so dom should have his car back tomorrow
