Thanks Evan!
FYI there is no CEL being thrown, only intermittent logs, but i've definitely noticed the car being a LOT less responsive recently, with a little low end jitter.
I had a quick check over the intake today and, after removing it, found that the screw at the bottom of the cone cover was missing! A guy in hardware at work found me the same M5 size, so i've popped this in. Everything was then re-torqued.
However: To disassemble the intake i was reading the install guide (
http://www.goapr.co.uk/support/vwr/VWR%20Fitting%20Cold%20Air%20Intake%20TFSI.pdf ). It mentions to use a square bracket for the front mount on the MK5, but the squishy scoop style mount for the Golf R/ed35 etc. Mine's been installed with the scoop style mount! It says MK5's should use the square bracket mount. Despite this, i'm not sure this would cause the issue, the car was running great for a while with the scoop mount.
So, i just ran 3 quick 3rd gear runs logging Misfire Sum, Cyl 1- 4, Lambda Sensor, Fuel Pressure, Boost (actual and specified) and fuel rail pressure (actual and specified), and Engine Speed (thanks bacillus!)
Bad news:
There was a misfire reported in Cylinder 3 on the end of the second run.
Good news:
Boost pressure actual seems to follow specified closely, but not for values lower than 1090mbar, i guess this is normal? I seem to remember seeing similar before the APR software flash.
I don't know much about fuel rail pressure, any hints? Looks like actual follows specified reasonably closely.
Download the log here:
https://gist.github.com/AnthonyMann/5961169/downloadI'll be taking the car back to Tuningwerkes as soon as i can, it's not a short trek. Really appreciate the input you guys might have on the logs if you have a min. Any obvious issues and solutions?
Thanks again!