So after going for my first turn of the key this week I encountered a MASSIVE water leak from the metal pipe the goes into a housing on the front of the block. After thinking about how to attack it as it's an absolute pig to get to I decided to remove the alternator to see if that made it easier, answer ........no
This meant only one thing, removal of the inlet manifold
One it was off I had a clear sight of it and upon removal the o-ring looked in good condition but I changed it for the new one and it worked perfectly even under a pressure test for 30 mins while I had breakfast
I bolted the whole car together and ran it up an it ran great so as from February It'll be getting some serious goodies. Custom exhaust and intake end of February, mapped end of March and then once ran in all well I'll start the interior.
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