FIXED..
To be honest, the below is irrelevant to most if not all of you on here, but i hate it when people dont post there results and fixes - especially if another member has given advise and it fixed it for them, yeah cheers mate
I am not one of those and i'll sure share anything i have to offer!
For some of you that may remember, i was experiencing and B*&tching a lot about my GTI having 4000rpm power cuts & stalling when cold temps was around. ONLY when cold.. if temps was above 10 degrees, no issues with power or stalling. To be more specific, if the ambient temperature was less than 10 degrees i would get power cuts almost like someone instantly turned the turbo off around the 4000rpm range. around 5 degrees or slightly lower the car would be really hesitant pulling away up until 1.5-2k rpm then it would be fine (then cut at 4000 lol) if the outside temp was 0 degrees or in the minus' the engine would start, idle then cut out and there wasn't anything i could do about it.. the throttle was completely disabled and wouldn't do anything! I also had really really bad turbo flutter but like a squealy screechy turbo squeal.. it would cha cha cha cha and then psshhh slightly at the end.. it done my nut in, was embarrassing! it wasnt even a nice flutter. it was almost like the DV wasn't working or delayed for a few seconds.
Anyway, in an attempt to find the fault.. i purchased VCDS at the start of the year to help me diagnose, but everything to my knowledge would match up and seemed to be working fine, i just couldn't work out what was going on. i crawled over the car trying to find anything mechanically wrong and couldn't. replaced all the common and some not so common parts and nothing made a difference. The only weirdest thing i came across that temporarily helped with every issue above was, if i disconnected the Intake Air Temperature sensor the car wouldn't stall in freezing temps, the throttle worked just fine and i had no power cuts at 4000rpm, the car drove absolutely fine (still had the annoying chatter) which made me sure, nothing mechanical was wrong and it had to be electrically related or at worst.. software related (map)!!
I do have a Ram Air intake and some people said the flutter would have been normal, but my mate and cousin both had the same car with the same intake and only ever had the "ppsshhh" never a flutter. so i couldn't see why mine would be any different. I always had a feeling the car had a remap but the previous owner said it didn't to his knowledge. after getting
@Pudding to read logs, help me diagnose, give me some pointers and advise me on where to look in VCDS to see if my engine had been flashed for sure.. we discovered it indeed had been mapped.
The chances of a map being corrupt is slim, but i didn't ignore this, i wanted to fully check the car to make sure i wasn't missing anything before having the map removed and ending up with the same problem only the car would be slower.
Well in the end, i couldn't figure it out.. the same issue kept pointing towards software or something electrical.. so i bit the bullet and took my car to a local garage to have a stock map file flashed onto the ECU so i can start again with a blank canvas! The result was brilliant!
I drove off down the road with
NO turbo flutter/chirpy squeals or weird screechy flutter noises changing gear and releasing throttle. All i hear now is "ppsshhh" which is expected and im happy with that (its not blow off loud) its resonated through the intake loud and im defo happy with that.
The day i had it done was 5 degrees, so blasted it..
NO power cuts at 4000rpm.. pulls right through fine.
couple of days later it was -2 in the morning, started the car up.. engine run fine and didn't stall, throttle was
NOT disabled and everything worked just fine.
more than happy and satisfied to say.. ALLLLL along, i had a bad map on the car (Shyyytttt software) or as
@Pudding said and i agree, the wrong map for the car was loaded on.. hence some issues! It's all fixed now though
Its really smooth now, the only downside is the power, i feel like im running 150hp not 200. i guess thats what a remap (@ 230-240 ish) spoils you with. i am going to smoke test and boost leak test to be sure its where it should be as i would say it feels slightly under powered and less punchy. i also need to do the inlet carbon clean (147k its way past needing it) and i experience a little rev hang still, so power and rev hang is my next mission but in no rush for now.
who would of thought it was software all along ey! thanks for reading if you made it this far. not a problem many people would come up against, but for those who ever wondered what was wrong with mine in the end... here you go lol enjoy